西南石油大学学报(自然科学版) ›› 2001, Vol. 23 ›› Issue (3): 47-49(5.DOI: 10.3863/j.issn.1000-2634.2001.01.014

• 石油工程 • 上一篇    下一篇

红岗油田复合驱先导性矿场试验

张忠林1 杨玉梅1 洪玲1 彭妥2 宣美乐3   

  1. 1.吉林油田分公司勘探开发研究院,吉林 松原 138001;2.中原油田陕北开发处;3.吉林油田分公司红岗采油厂
  • 收稿日期:2000-11-20 修回日期:1900-01-01 出版日期:2001-08-20 发布日期:2001-08-20
  • 通讯作者: 张忠林

ASP FLOODING PILOT TEST IN HONGGANG OILFIELD

ZHANG Zhong-lin1 YANG Yu-mei1 HONG Ling1 et al   

  1. Exploration & Exploitation Research Institute of Ji Lin Branch of Oilfield Company, Songyuan Jilin 138001,China
  • Received:2000-11-20 Revised:1900-01-01 Online:2001-08-20 Published:2001-08-20
  • Contact: ZHANG Zhong-lin

摘要: 红岗油田目前的注采井网和注水方式已基本上满足了油田开发的需要,依靠常规技术提高采收率的难度越来越大,有必要探索出一种适合红岗油田实际情况的三次采油方法。经过室内研究和矿场试验证实:在红岗油田进行复合驱是可行的。矿场试验情况表明:三元复合驱技术是适合于红岗油田萨尔图油层的,尤其对剩余油饱和度较大、非特高含水井的效果非常显著。另外在国内首次把复合驱技术应用于注采井距大的反十三井网中,为红岗油田稳产高产提供了一条新的途径。

关键词: 提高采收率, 复合驱, 先导性试验, 动态分析, 红岗油田

Abstract: It is more and more difficult to enhance oil recovery in Honggang oilfield through conventional technology based on the existing well pattern and configuration. So it is increasingly necessary to seek for a suitable tertiary oil recovery method to improve ultimate recovery. The lab experiments and oilfield pilot test show that ASP flooding is most practical in Hong Gang oilfield. The pilot test also indicates that the ASP flooding effect is most remarkable in high remaining oil saturation and/or low watercut reservoir. It is the first time for the ASP technology to be applied to the sparse reverse 13-point well pattern, which is another way to maintain and even to enhance the oil rate of Honggang oilfield.

Key words: enhanced oil recovery, ASP flooding, performance analysis, pilot test, Honggang oilfield

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