西南石油大学学报(自然科学版) ›› 2023, Vol. 45 ›› Issue (6): 125-134.DOI: 10.11885/j.issn.1674-5086.2021.10.21.32

• 石油与天然气工程 • 上一篇    下一篇

可溶筛管在塔里木油田高温高压气井中的应用

魏军会1, 景宏涛1, 谢英2, 李建明1, 司想1   

  1. 1. 中国石油塔里木油田油气工程研究院, 新疆 库尔勒 841000;
    2. 中国石油塔里木油田克拉采油气管理区, 新疆 库尔勒 841000
  • 收稿日期:2021-10-21 发布日期:2024-01-06
  • 通讯作者: 魏军会,E-mail:wjhui-tlm@petrochina.com.cn
  • 作者简介:魏军会,1989年生,男,汉族,陕西咸阳人,工程师,硕士,主要从事采油、采气工程等方面的研究工作。E-mail:wjhuitlm@petrochina.com.cn;景宏涛,1981年生,男,汉族,新疆库尔勒人,高级工程师,主要从事高压油气井采油气工程方面的研究工作。E-mail:jinghongtaotlm@petrochina.com.cn;谢英,1981年生,女,汉族,四川内江人,高级工程师,主要从事油气田开发采油气方面的研究工作。E-mail:jingmingmei@126.com;李建明,1975年生,男,汉族,山西曲沃人,高级经济师,主要从事油气田开发等方面的工作。E-mail:lijm-tlm@petrochina.com.cn;司想,1994年生,男,汉族,新疆塔城人,工程师,硕士,主要从事采气工艺方面的研究工作。E-mail:sixiang-tlm@petrochina.com.cn

Application of Dissolvable Screen Pipe in HTHP Gas Well in Tarim Oilfield

WEI Junhui1, JING Hongtao1, XIE Ying2, LI Jianming1, SI Xiang1   

  1. 1. Oil and Gas Engineering Research Institute, Tarim Oilfield Company, PetroChina, Korla, Xinjiang 841000, China;
    2. Kela Oil and Gas Production Administrator Area, Tarim Oilfield Company, PetroChina, Korla, Xinjiang 841000, China
  • Received:2021-10-21 Published:2024-01-06

摘要: 为解决塔里木油田高温高压气井清洁完井及砂埋井快速修井的问题,研发了一种可酸溶形成生产通道的可溶筛管,可实现充分替液,达到清洁完井的目标。同时,可溶筛管与封隔器下部管柱使用销钉连接,在修井作业中,可实现分段打捞,减少作业量,降低作业周期,降低作业风险,提高修井效率,从而减小修井作业对储层的伤害。对可溶筛管进行了室内评价,该筛管使用的可酸溶材料在温度达110 ℃时,所有厚度试样均全部溶解,物理性能也可以满足抗内压35 MPa,持续稳压15 min的密封设计要求,在650 kN抗拉载荷实验中筛管无变形,满足现场施工要求。在现场应用的井中,产能恢复率平均达211.0%,远高于以往的78.1%,实现了低成本清洁完井及后期安全修井作业,该技术的应用前景良好。

关键词: 高温高压, 可溶筛管, 清洁完井, 销钉连接, 分段打捞

Abstract: In order to solve the problem of clean completion of high temperature and high pressure gas wells and rapid workover of sand buried wells in Tarim Oilfield, a dissolvable screen pipe has been developed that can be acid dissolvable to form a production channel, which can achieve the goal of clean completion by fully replacing the fluid. The dissolvable screen pipe is connected to the lower tubing column of the packer by pins, which can be fished in sections during workover operations, reducing the workload, lowering the workover cycle, reducing the risk and improving the workover efficiency, thus reducing the damage to the reservoir during workover operations. The material dissolved in all thicknesses at a temperature of 110 ℃. The physical properties also met the seal design requirements of 35 MPa internal pressure test and 15 min continuous steady pressure, and no deformation in the 650 kN tensile load test. In the three wells applied in the field, the average recovery rate of 211.0% was much higher than the previous 78.1%, achieving the effect of low-cost clean completion and safe repair operation later, which provides a good reference for the application effect of this technology.

Key words: HTHP, dissolvable screen pipe, clean well completion, pin connection, sectional fishing

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