西南石油大学学报(自然科学版) ›› 2004, Vol. 26 ›› Issue (4): 25-27.DOI: 10.3863/j.issn.1000-2634.2004.04.007

• 石油与天然气工程 • 上一篇    下一篇

葡北油田气水交替注烃混相驱开发研究

郭平1 杜志敏1 张茂林1 王仲林2 孙玉凯2 谭光天2 刘滨2   

  1. 1.“油气藏地质及开发工程”国家重点实验室(西南石油学院),四川成都610500; 2.中国石油吐哈油田
  • 收稿日期:2003-01-21 修回日期:1900-01-01 出版日期:2004-08-20 发布日期:2004-08-20
  • 通讯作者: 郭平

CASE ANALYSIS ON HYDROCARBON ALTERNATIVE GAS MISCIBLE FLOODING IN PUBEI OIL FIELD

GUO Ping DU Zhi-min ZHANG Mao-lin WANG Zhong-lin SUN Yu-kai TAN Guang-tian LIU Bin   

  1. Southwest Petroleum Institute, Chengdu Sichuan 610500, China
  • Received:2003-01-21 Revised:1900-01-01 Online:2004-08-20 Published:2004-08-20
  • Contact: GUO Ping

摘要: 对我国第一个注烃混相驱开发的砂岩油田葡北油田进行实例分析,该油田储层渗透率110.5×10-3μm2,构造完整,连通性好,断裂系统不发育,属典型挥发性油藏,最小混相压力(MMP)为33 MPa,注入气为油田伴生气。长岩心的实验表明先注气比先注水原油采收率更高,为了对比先注气还是先注水好,采用东边先注水西边先注气的开发方式,地层压力保持在35 MPa,早期采用7采8注共15口井开发,到目前有采油井9口,注气井2口、注水井7口;区块日产油44 t,日注水144 m3,日注气14.55×104m3,到2001年10月,已开发3年,原油采出程度19.05%,油田综合含水3%,有部份井气油比有所上升,但未出现气明显突破现象。设计是气水交替,但由于水井转注气注不进而未能实施。介绍了油田地质概况、基础研究实验、方案设计、开发情况、动态监测、实施中存在的问题等,并提出了相关建议,分析结果对类似的油藏混相驱开发有一定指导意义。

关键词: 低渗油藏, 注烃混相驱, 气水交替

Abstract:

The oil field in China with the method of development by miscible flooding is scare, to sum up the experiences, this paper analyses the developments of Pubei oil field which is the first sand oil reservoir to perform hydrocarbon miscible flooding in China. It has integrated, good connecting formation with undeveloped cracking system and permeability of 110.5×10-3μm2.
It is a typical volatile oil reservoir. The minimum miscible pressure (MMP) is 33MPa. The Injected gas is the by-produced gas in the oilfield. The results of core flooding experiments showed that oil recovery by primary gas injection is higher than primary water injection. To chose one best method, the field
was developed by primary water injection at east and primary gas injection at west, keeping formation pressure at 35MPa. At early exploration time, there were seven injection wells and eight production wells. Now, there are nine production wells and two gas injection wells, seven water injection wells. The
velocity of oil production is 44t/d, gas injection is 14.55×104m3/d, water injection is 144m3/d. It has developed for three years till October 2001; the oil recovery is 19.05%, the synthetic water saturation is 3%. There are certain increases of GOR in some production well but no obvious gas breakout. Pri-
mary water injection well cannot change to gas injection since gas cannot be injected after water injection, so cannot perform GAW in east area. This paper introduces general geometry character, basic experimental study, exploration performance, and existing problem of the reservoir and gives some proposals,
which is helpful in exploration the similar oil reservoir by miscible flooding.

Key words: low permeability reservoir, hydrocarbon miscible flooding, WAG

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