西南石油大学学报(自然科学版) ›› 2022, Vol. 44 ›› Issue (4): 62-70.DOI: 10.11885/j.issn.1674-5086.2022.03.07.02

• 石油与天然气工程 • 上一篇    下一篇

低渗致密油藏适度温和注水技术研究与矿场实践

王香增1,2, 高涛2,3, 梁全胜3, 党海龙2,3   

  1. 1. 陕西延长石油(集团)有限责任公司, 陕西 西安 710065;
    2. 陕西省特低渗透油气田勘探与开发工程技术研究中心, 陕西 西安 710065;
    3. 陕西延长石油(集团)有限责任公司研究院, 陕西 西安 710065
  • 收稿日期:2022-03-07 发布日期:2022-07-28
  • 通讯作者: 王香增,E-mail:sxycpcwxz@126.com
  • 作者简介:王香增,1968年生,男,汉族,河南滑县人,教授级高级工程师,博士,主要从事特低渗油气开采工程技术研究工作。E-mail:sxycpcwxz@126.com
    高涛,1988年生,男,汉族,陕西延安人,高级工程师,硕士,主要从事油气藏工程研究。E-mail:gaotao95@163.com
    梁全胜,1978年生,男,汉族,新疆奎屯人,教授级高级工程师,博士,主要从事油气勘探开发地质与地球物理综合研究工作。E-mail:liangqsh0833@163.com
    党海龙,1971年生,男,汉族,陕西渭南人,教授级高级工程师,主要从事特低渗透油田开发工作。E-mail:danghl71@qq.com
  • 基金资助:
    陕西省科技统筹创新工程计划(2011KTZB–04)

Research and Field Practice of Moderate Mild Water Injection Technology in Low Permeability Tight Reservoir

WANG Xiangzeng1,2, GAO Tao2,3, LIANG Quansheng3, DANG Hailong2,3   

  1. 1. Shaanxi Yanchang Petroleum(Group) Co. Ltd., Xi'an, Shaanxi 710065, China;
    2. Shaanxi Ultra Low Permeability Oil and Gas Exploration and Development Engineering Research Center, Xi'an, Shaanxi 710065, China;
    3. Research Institute of Shaanxi Yanchang Petroleum(Group) Co. Ltd., Xi'an, Shaanxi 710065, China
  • Received:2022-03-07 Published:2022-07-28

摘要: 为解决低渗致密油藏注水过程中,水相沿着裂缝水窜水淹、基质原油难采出、水驱采收率低等技术难题,以鄂尔多斯盆地延长组长6储层为研究对象,开展驱替速度对水驱采收率影响的驱替实验并进行核磁测试分析,建立考虑毛管力的非稳态油-水两相水驱前缘推进数学模型,形成适度温和注水强度优化图版。结果表明,水驱油过程存在最佳驱替速度使得水驱采收率最大,实验中最佳驱替速度为0.06~0.08 mL/min。以延长油田ZC区块为例,调整注水强度为0.85~1.20 m3/(d·m),采油泵沉没度控制在100~150 m,技术应用后水驱采收率从20%提高到24%。适度温和注水技术对低渗致密油藏提高采收率效果显著,研究成果为类似油藏高效注水开发提供了借鉴。

关键词: 适度温和注水, 渗吸-驱替双重作用, 水驱前缘模型, 低渗致密油藏, 提高采收率

Abstract: In order to solve the technical problems of water phased channeling and flooding with fracture water, difficulties in recovery of matrix crude oil and low water drive recovery in ultra-low permeability tight reservoirs during water injection. In order to explore the effect of displacement rate on water drives recovery, we carry out the displacement experiment taking Chang-6 Reservoir of Ordos Basin as the research object. Then the NMR test results are analyzed, finally, the unsteady oilwater two-phase water flooding front propulsion mathematical model considering capillary force is established to form the policy method of moderate water injection technology. The results show that there is an optimal displacement rate in the process of water flooding, which makes the water flooding recovery maximum. The best displacement rate in the experiment is 0.06~0.08 mL/min. Taking the ZC Block of Yanchang Oil Production Plant as an example, moderate technical policies is adopted to control the water injection intensity in the block of 0.85~1.20 m3/(d·m), and the submergence of the oil pump is controlled at 100~150 m. After the application of the technology, production data show that the water flooding recovery is increased from 20% to 24%. Moderate mild water injection technology has a significant effect on EOR of low-permeability tight reservoir. The research results provide a reference for similar reservoirs in the process of high-efficiency water injection development.

Key words: moderate water injection, imbibition displacement dual action, water driven front model, ultra-low permeability tight reservoirs, EOR

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