西南石油大学学报(自然科学版) ›› 2005, Vol. 27 ›› Issue (5): 37-39.DOI: 10.3863/j.issn.1000-2634.2005.05.10

• 石油与天然气工程 • 上一篇    下一篇

K稠油油藏开采优化数值模拟研究

张啸枫 张烈辉 冯国庆   

  1. “油藏地质及开发工程”国家重点实验室(西南石油学院),四川 成都 610500
  • 收稿日期:2004-10-09 修回日期:1900-01-01 出版日期:2005-10-20 发布日期:2005-10-20

RESEARCH ON THE K HEAVY O IL RESERVO IRW ITH OPTIM IZING NUMERICAL SIMULATION

ZHANG Xiao-feng ZHANG Lie-hui FENG Guo-qing

  

  1. State Key Laboratory ofOil and Gas ReservoirGeology and Exploitation·SouthwestPetroleum Institute, Chengdu Sichuan 610500, China
  • Received:2004-10-09 Revised:1900-01-01 Online:2005-10-20 Published:2005-10-20

摘要:

我国西部K油藏为浅层稠油油藏,油层平均埋深240m,属于边缘氧化型稠油油藏。针对K油藏开发过程中注入蒸汽波及的效率低,热连通不充分,油汽比低,经济效益差的现状,选择该油藏有代表性的井组,利用数值模拟方法,对该油藏连续汽驱、间歇汽驱、低干度汽驱等技术方案进行了深入的研究,综合经济因素和最终采收率确定了合理的开发方案为高注汽强度的间歇汽驱,注汽强度80~100m3/d,注汽周期为6个月。数值模拟结果对油田实际开发有指导作用。

关键词: 汽油比, 数值模拟, 蒸汽驱, 历史拟合

Abstract: TheK reservoir is a typical shallow heavy oil reservoir in westChinawith average depth of 240m and belonging to fringe oxygenation heavy oil reseavoir. Aimed at the low sweep efficiency of the injected steam, the deficient heat connect and the bad economic benefit in the producing process ofK reservoir, atypicalwell group was chose for studying. W ith the application of reservoir numerical simulation, a detailed study is done on technique plans which could be applied in K reservoir such as steam flooding, intermittent steam flooding, low quality steam flooding and so on. Combine the economic factorswith the final oil recovery efficiency of every plan 's results, it is recognized that the reasonable plan is intermittent steam flooding. The reasonable steam injection rate is 80-100 m3/d and the injection cycle is sixmonths. Results of the numerical simulation should be consulted in the reservoir exploitation.

Key words: steam oil ratio, numerical simulation, steam flooding, historymatching

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